Dear all,
I have assembled quadcopter with following details:
Turnigy 1400kv brushless motor
30A ESCs
Kkmulticopter V5.5 circuit board
10*4.5 propelles
CT6B transmitter
2200mah 3cell 25C battery
My concern is the quad is wobbling at the time of take off!
I have never tested the flight b'coz it never took off!
I am a beginner! Please suggest remedy!
The gains r high
hi..!!
How to lower those with KKmultirotor V5.5 ??? ??? ???
Reduce the pitch gyro on the kk board with a small screwdriver. Hopefully it should do the trick