Hi all i have purchases Reptile 500 ARF Kit. I am getting problem in fly quad copter. every this connected properly & all controls are working fine but issue with flying. after given full throttle quad not flying. it's stay on ground only. Please suggest me.
Technical details & image given below:-
1.XY500 Reptile frame x 1.
2.Avionic Hexa Quad controller.
3.SunnySky 2212 980KV motors x 4.
4.SimonK 30A ESC x 4.
5.1045 Propeller x 2 pairs.
6.Batter 2600mah 11.1v, 35C.
Is there any jitter in the motors while spinning??
No
if u hv more experience on quad then can u come online on chat? plz
if u hv more experience on quad then can u come online on chat? plz
You can contact the rcbazaar.com to solve your problems.. I am not quite experienced with avionic hexa quad fc
according to you what is prblm? esc or motor issue or anything else?
Can you post a video on what is happening
give me ur mail id i will share with u.
Check pm
video size is 45Mb not possible on whatsapp. it's already uploaded on my drive. give me ur mail id i will share with u.
Okay
Check if motors are spinning in right direction.
Props seems OKAY!
check ur mail i hv share with u.
yes all r connected right direction.
Check again... check if the motors are spinning in the correct direction and if the right prop is on the right motor. .. I think this has to be the reason why it is not lifting off
What Voltage are you getting from that battery at fully charged state?
11V
Are you using a 3S lipo? If so the full charge voltage for 3S lipo is 12.6V. 11V is too less!!
I suppose 11.1v is 3s
Batter 2600mah 11.1v, 35C.
Run the props (be careful)just put tour hand under and above the running prop.. if the amount of air is more on the upper side.. The prop is wrong
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If its the KK2 , then yes i may be able to help you :)
Just contact anywhere you want :)
@jeet8066,
Another member had a similar problem recently.
On looking at his video carefully, i found that the airflow was upwards!
The props were pushing the quad into the ground!
Normally it should show a tendency to lift near half throttle.
No way you can use full throttle without hitting the roof!
Your prop position appears correct.
Check that front left motor runs clockwise when seen from above. I suspect it goes anticlockwise!
yes ... assuming that the white are the back and the black are the front, you have the props set-up in the opposite direction
Quote from: parichya.gautam on April 30, 2015, 12:26:00 PM
yes ... assuming that the white are the back and the black are the front, you have the props set-up in the opposite direction
May I differ?
Irrespective of whether white arms are front or back,
Top left prop is clockwise, ie correct.
Motor may be CCW, ie incorrect.
Assuming that in the photo, 'Front' is either to the left or right side of the photo.
Hi @ KK please find attachment.
yes, its all a matter of perspective . let the OP confirm it i guess..
Guys share me ur mail id i will share u video.
Jeet, don't just go by the specs. 11.1v is the nominal voltage for 3S LiPo Packs. While at fully charged state it would be about 12.6volts.
If you have a multimeter or a LiPo Alarm then please first charge the battery to the full and then measure the voltage.
If the voltage that you are getting is substantially lesser than 12.6 volts (11V is way too low) then the reason of your quad not being able to leave the ground would be a Discharged/Damaged battery which happens when people allow LiPo packs to get fully discharged.
Please confirm.
@jeet wouldn't it be better if you put the video on the page itself(as you have uploaded on Drive) rather than sending the link to the video personally? Less time consuming and ppl with similar problems might be benefited and someone might be able to solve the problem quickly? :hatsoff:
Are the ESC properly calibrated upto the endpoints?
yes all configuration are proper & all motors are starts same time.
video url- https://drive.google.com/file/d/0B4BZPQF3jsgWRFVjRWc4Y3pqaUk/view?usp=sharing
I think you have mounted the props in the wrong direction cw props on ccw turning motor(as KK Iyer Sir suggested).....put the throttle at 20-30% and by putting the hand over the prop(BEWARE: keep safe distance!!!!) if you feel the air hitting you hand you have mounted the props in the wrong place
Check in which direction the motors are spinning
This might help
(http://www.pyramidmodels.com/shop/shopimages/props%20rotation.jpg)
Hello Jeet. I am assuming you have carried out all the steps involved in setting up the flight controller as referenced in the manual here (https://drive.google.com/file/d/0B4saiZvhGj-CejBRSU1HdHVfQWM/edit) as you are able to arm the quadcopter and spin the motors. This means the problem is probably due to motor direction or a battery issue. The propellers have been mounted correctly as per the photograph. Please verify whether each motor is actually spinning in the correct direction. And what is the battery voltage and individual cell voltages now?i
ok today i will check again.
@jeet8066,
Props and rotation ARE OK.
Don't fiddle with it.
Weight too much, or battery low.
Why is it flashing? Indicating low voltage?
To me it looks like low voltage or ESCs not caliberated, hence not recognising full throttle.
Before you do anything else, just post the battery voltage.
Motor is armed hence light is flashing & weight is also very less. i this issue with battery.
First i would like to say thank to all!! now my quad flying! issue with battery after i got B6 charger i come to know that battery one cell was dead & i am getting 10V only. Now issue resolved.
Happy Flying...
Video of flying?? ;) (:|~ {:)}
Definitely i will share video with you guys.